Year |
Date |
Facility |
Overview |
Report
Classification |
2010 |
April
2 |
Onagawa
1 |
Damage
to a pipe joint in the standby liquid control system accumulator. |
|
|
April
2 |
Shika
1 |
Primary
loop recirculation system flow restrictor device alarm activated. |
|
|
April
12 |
Hamaoka
5 |
In
a confirmation test following re-modelling of the control rod block monitor,
when the withdrawal of control rod numbers 34-03 above the fully withdrawn
position (100 steps) was implemented, the "coupling" display should
normally have lit up when the control rod was over-withdrawn to the 102nd
step. However, at step 101, the "control rod withdrawal prevention"
alarm light came on and the control rods stopped. It has been confirmed that
the interlock had failed. |
|
|
April
19 |
Mihama
2 |
Rise
in the concentration of radioactivity in the primary coolant due to leaks
from two fuel assemblies. |
|
|
April
20 |
Mihama
5 |
Fractures
in the welding on the moisture separator and reheater (B). |
|
|
April
25 |
Mihama
2 |
Rise
in reading on the containment exhaust gas monitor when extracting air from
inside the containment. The cause was found to be coolant leaking from the
primary coolant pump B. |
|
|
April
27 |
Ikata
1 |
Damaged
piping in the seawater coolant for the emergency diesel generator (B). |
Law |
|
May
20 |
Onagawa
1 |
Discovery
of a fracture, 30 mm long, 5.2 mm deep, in one location when 6 locations on
the recirculating system piping welds were inspected. |
|
|
May
31 |
Fukushima
Daiichi 1 |
When
measuring condensate system pipe wall thickness, a value (7.6 mm) less than
the minimum required thickness (8.3 mm) was detected. |
|
|
June
1 |
Fukushima
Daini 1 |
When
confirming the opening and closing of the isolation valve inside steam piping
in the reactor core isolation cooling (RCIC) system during a regular
inspection, a problem was experienced with the valve not opening fully. The reactor was shut down
manually for an inspection. |
Law |
|
June
2 |
Shika
2 |
Alarm
activated to indicate abnormality in the detector monitoring the degree of
opening of the main steam stop valve (D). |
|
|
June
4 |
Hamaoka
4 |
Of
the main turbine shaft vibrations, a slight rising trend was confirmed in the
shaft vibration values in the bearings (No.7 or No.8 bearings) of the
low-pressure turbine (C). |
|
|
June
11 |
Ikata
1 |
Damage
to the seawater coolant piping of the component cooling water heat exchanger
(A). |
Law |
|
June
15 |
Tsuruga
1 |
It
was discovered in an inspection of a welded ferrule on the recirculation pump
casing that there was a weld line on the pressure-containing section of the
recirculation pump that was not shown in the blueprints and was also missing
from the items on the in-service inspection. |
|
|
June
17 |
Fukushima
Daiichi 2 |
As the "generator field
circut breaker trip alarm" was activated, the generator protection
device was also activated causing the generator to shut down, and the turbine
and nuclear reactor also automatically shut down. As the changeover to the plant's
power source system did not occur and the plant's power system stopped, the
emergency diesel generators were activated and a transient phenomenon
occurred where the water level in the reactor was greatly reduced. |
|
|
June
17 |
Shika
1 |
Fracture in the
welding of the recirculation pump (B) outlet valve on the leak disposal
system piping. |
|
|
June
24 |
Shika
1 |
Trouble occurred when
inserting one control rod after removal of all fuel from the reactor. |
|
|
June
25 |
Tokai
Daini |
In
a regular inspection of two seawater pumps (B and D) of the residual heat
removal system, the value of the seawater flowmeter was found to be below the
standard value. The reactor was shut down manually when it proved to be
impossible to specify the cause of the low reading after dismantling and
checking the pumps. |
Law |
|
July
7 |
Fukushima
Daini 1 |
An
inspection tool fell into the nuclear reactor during inspection work on the
Local Power Range Monitor. |
|
|
July
7 |
Fukushima
Daiichi |
It
was confirmed that the pressure reading on the device (pressure guage) system
monitoring the cask sealed gas inside one of four medium-sized dry casks in
the cask storage building at Fukushima Daiichi Nuclear Power Station was
downscaling. Downscaling means the reading dropped to the lowest level. |
|
2010 |
July
11 |
Fukushima
Daini 1 |
A
foreign object was found on the baffle plate in the vicinity of jet pump No.1
in the nuclear reactor. |
|
|
July
16 |
Fukushima
Daini 1 |
While
replacing valves on the residual heat removal system instrumentation system
line valves, indicating patterns were confirmed on four of the valve casings
when penetrant tests were performed on the welds. |
|
|
July
28 |
Fukushima
Daiichi 3 & 4 |
Gamma-emitting
substances (Silver-110m, Cobalt-60, Manganese-54) were detected on sampling
filters taken from the main exhaust stack between July 28 and August 4. |
|
|
July
30 |
Rokkasho
Reprocessing Plant |
High-level
radioactive liquid waste leaked into the protective pipe on the thermometer
on the high-level liquid waste concentration tank in the separation building.
This was due to corrosion in the lower part of the concentration tank. |
Law |
|
August
4 |
Fukushima
Daiichi 1 |
Confirmation
of damage and missing parts in the support structure for the downstream
piping for the return valve in the high-pressure injection system startup
test return piping. Confirmation also of eight cases of damage and missing
parts in the support structure in other locations. |
|
|
August
12 |
Fukushima
Daiichi 1 |
Water containing radioactive
substances was confirmed to be dripping from the vicinity of the lower part
of the high-pressure turbine casing to the vicinity of the feedwater heater
area on the 1st floor of the turbine building (controlled area) and the reactor
was shut down manually to investigate this. |
|
|
August
21 |
Kashiwazaki-Kariwa
1 |
The degree of
vacuum of the condenser declines and a variation in power output of max.
13,000 kW occurred. It was confirmed that the water box communication valve
was in the fully open position, whereas the condenser (B) should normally be
in a totally closed state. |
|
|
August
23 |
Fukushima
Daiichi 3 |
Subcontractor
workers were polluted and suffered internal exposure when carrying out a
dismantling inspection of a valve in the reactor building pressure
suppression chamber area (controlled area). |
|
|
August
26 |
Onagawa
3 |
When implementing the
dismantling inspection of scram outlet valves in 137 control rod drive
hydraulic system hydraulic control units, the valve shaft slide on two of the
units were confirmed to be damaged. |
|
|
August
26 |
Monju |
While being
hoisted out of the reactor, an in-vessel transfer machine was deformed when
dropped back into the reactor. |
Law |
|
September
2 |
Fukushim
Daiichi 5 |
When implementing the monthly
regular inspection of the reactor core isolation cooling system, a turbine in
the same system automatically stopped. It was confirmed that the signal cable
controlling the steam governing valve, which governs the amount of steam
being provided to the turbine, was disconnected. |
|
|
September
7 |
Hamaoka
5 |
Reheat cracks
found in the moisture separator & reheater outlet pipe welds. |
|
|
September
10 |
Kashiwazaki-Kariwa
7 |
Rise
in the reading of the high-sensitivity off-gas monitor on the off-gas system.
Leak confirmed from one fuel assembly. |
|
|
September
14 |
Fukushima
Daiichi 6 |
When
conducting a confirmation test for leaks in one gas-side system in the
flammable gas concentration control system, it was found that the test
pressure could not be maintained. |
|
|
September
25 |
Fukushima
Daini 3 |
Power
output fell to 380,000 kW due to the occurrence of an incident in which a
large amount of seaweed etc. was taken into the intake screening device on
the seawater intake for the turbine condenser coolant seawater. |
|
|
September
27 |
Onagawa
3 |
Damage
to the accumulator of one water pressure control unit of the control rod
drive mechanism. |
|
|
October
1 |
Tomari
2 |
A
fluctuation of the concentration of boric acid occurred due to a disorder in
the temperature control of the extraction line nonregenerative heat exchanger
observation outlet. |
|
|
October
4 |
Onagawa
1 |
An
alarm was activated in the central control room indicating inability to
operate devices for containment radiation detection for the containment
atmosphere monitoring system monitor. |
|
|
October 14 |
Hamaoka 4 |
Temporary
operational aberration due to faulty operation of the startup range monitor. |
|
|
November
1 |
Kashiwazaki-Kariwa
7 |
Fractures
were discovered in the sheaths and tie-rods of 28 hafnium flat tube type
control rods. |
|
|
November
1 |
Mihama
2 |
During
a regular inspection of the reactor containment air recirculation fan, when
one of the air recirculation fans was started up the cooling water intake
valve and discharge valve of the D-containment air handling device cooling
coil should have opened automatically upon receipt of the startup signal, but
a problem occurred in the form of the discharge valve not opening. |
|
|
November
2 |
Fukushima
Daiichi 5 |
During
work to reduce power output in order to adjust the control rod pattern, the
water level in the reactor core rose and fell rapidly, causing the turbine to
go into automatic shutdown followed by automatic shutdown of the reactor. |
Law |
|
November
4 |
Kashiwazaki-Kariwa
5 |
During
a manual startup of diesel generators for a regular inspection of the
high-pressure reactor core spray system, the alarm "HPCS diesel
generator equipment failure" occurred in the central control room and
the alarm "generator overvoltage" occurred at the control panel at
the location. |
|
|
November
25 |
Fukushima
Daini 4 |
A fracture was discovered in one
location in the base metal that had separated from the weld line of the
inside of the middle shell region of the reactor core shroud. |
|
|
December
1 |
Kashiwazaki-Kariwa
3 |
During work to
restore the control rod drive mechanism, the control rod drift alarm occurred
when the worker at the site operated the drive water pressure system valve
for control rods 38-59. Although they should have been in the fully withdrawn
position, it is thought that trouble had occurred when returning the control
rods to their original position after inserting them by one notch. It is
assumed that air had entered the piping of the control rod drive system. |
Law |
|
December
1 |
Shika
1 |
Due
to discovery of damage to the mechanical seal on a recirculation pump, the
reactor was manually shut down to replace the mechanical seal. |
|
|
December
7 |
Shika
1 |
A
worker was sprayed with water during work to replace the mechanical seal on a
recirculation pump. |
|
|
December
8 |
Hamaoka
3 |
During
the implementation of an inspection of a steam dryer, a fracture was
confirmed in the proximity of a weld on the steam dryer. |
|
|
December
10 |
Genkai
3 |
Occurrence
of a rise in the concentration of iodine in the primary coolant. A leak in
one fuel assembly (uranium fuel) was confirmed. |
|
|
December
11 |
Global
Nuclear Fuel Japan |
The
temperature adjustment device on a gadolinia sintering furnance (B) in
operation failed to work correctly. During work to restore the device,
heating ceased due to activation of the interlock for the heating limit, and
operation of the sintering furnace was stopped manually. |
Law |
|
December
13 |
Shika
1 |
During reactor startup, when the
operation for the withdrawal of one control rod was implemented, the
"control rod drift" alarm was activated, and the problem that the
rod was withdrawn 3 notches beyond the scheduled withdrawal position of 2 notches
occurred. The reactor was manually shut down for inspection. |
|
|
December
20 |
Hamaoka
4 |
Fractures were
discovered in three places in the proximity of the welds on the suspension
rod and support ring of a steam dryer. |
|
|
December
26 |
Fukushima
Daini 4 |
A
problem of decrease in the water level in the spent fuel pool occurred. |
|
|
December
27 |
Onagawa
3 |
Rise
in the concentration of radioactive substances in the off-gas system and
confirmation of a leak in one of the fuel assemblies. Bulging was found in
the cladding of one of the fuels rods in the relevant fuel assembly. |
|
|
December 28 |
Monju |
Damage
found in seven places in the cylinder liner of an emergency deisel generator. |
Law |
2011 |
January 9 |
Tomari
3 |
One worker was confirmed as
having body contamination by radioactive substances when implementing a
change of filter element on the 3B-coolant demineralizer intake filter in the
reactor auxilliary building, and this was confirmed to include internal exposure
of radioactive substances by whole body counter. |
|
|
January
18 |
Shimane
1 |
Regarding
69 weld locations on piping, etc, in the primary recirculation system, when
implementing an inspection for damage by ultrasonic test, fractures were
discovered on January 18 in one location on the weld joint on the downstream
piping of the A-primary recirculation pump discharge valve, and on February
17 in one location on the weld joint on the upstream piping of the A-primary
recirculation pump intake valve. |
|
|
January
21 |
Shika
2 |
Manual
shutdown of reactor due to reduction in the amount of condensation in the
containment inner heat exchanger. |
Law |
|
January
21 |
Hamaoka |
Occurrence
of control rod drift due to poor assembly of the control rod drive water
pressure system accumulator. |
|
|
January
27 |
Fukushima
Daiichi 1 |
Power
output manipulation due to restart of reactor water clean-up system. |
|
|
January
31 |
Kashiwazaki-Kariwa
1 |
Departure
from operation limits due to symptoms of failure in the operation of the
recirculation flow control valve on the flammable gas concentration control
system. |
|
|
February
2 |
Fukushima
Daini 3 |
Departure
from operation limits due to inspection of equipment related to emergency
deisel generators (B). |
|
|
February
3 |
Shika
2 |
Defect
found when starting power source for the drive of the control rod drive
mechanism during equipment checking work while plant was in shutdown. |
|
|
February
8 |
Mitsubishi
Nuclear Fuel |
Uranium
dioxide powder leaked from extraction device in the conversion and processing
room of the conversion factory. The leak amounted to 5.5 x 10^5 Bq. Four
workers were exposed to a maximum of 4.98 mSv. |
Law |
|
February
14 |
Ikata
3 |
As
it was found that there was a delay when performing the release operation of
the reactor trip breaker, the circuit was replaced. |
|
|
February
17 |
Tomari
3 |
Damage
on the solenoid valve terminal block for the cooling water flowrate
changeover valve on the control air compressor. |
|
|
February
21 |
Kashiwazaki-Kariwa
6 |
Contamination
by radioactive substances on the floor of the reactor building pump room. |
|
|
February
25 |
Genkai
2 |
Pipe
wall thinning exceeding the standard was found on the inner surface of five
SG tubes in the component cooling water heat exchanger. |
|
|
February
28 |
Shika
1 |
Reactor
shut down manually due to replacement of shaft seal on the reactor coolant
recirculation pump (B) |
|
|
March
7 |
Ikata
3 |
The
reading of the central control room radioactivity measurement monitor
temporarily rose to 60 µSv/h (alarm set to activate at 2.6 µSv/h), and the
central control room ventilation system isolation was operated. |
|
|
March
8 |
Higashidori
1 |
Damage
on the pressure guage of the control rod drive mechanism pressure control
unit. |
|
|
March
11 |
Fukushima
Daiichi |
Great
East Japan Earthquake: Units 1, 2 and 3 go into automatic shutdown. Later,
due to loss of all alternating current power, reactor core meltdowns and
hydrogen explosions occur and massive amounts of radioactive substances were
released into the environment. |
Law |
|
March
11 |
Fukushima
Daini |
Great
East Japan Earthquake: Units 1, 2, 3 and 4 go into automatic shutdown.
Function of pressure suppression chamber temporarily lost. Reactor core
damage was closely avoided due to maintenance of one external power source. |
Law |
|
March
11 |
Tokai
2 |
Great
East Japan Earthquake: Large vibrations in turbine cause reactor to shut down
automatically. Reactor core damage closely avoided due to function of
emergency diesel generators. |
Law |
|
March
11 |
Onagawa |
Great
East Japan Earthquake: Units 1, 2 and 3 go into automatic shutdown. A fire
occurred in the power panel and the emergency diesel generators stopped.
Reactor core damage was closely avoided due to ability to secure one external
power source. |
Law |
|
March
11 |
Higashidori |
Great
East Japan Earthquake: Down for regular inspection. Due to loss of external
power source, power was supplied by emergency diesel generators. |
|
|
March
11 |
Rokkasho
Reprocessing Plant |
Great
East Japan Earthquake: Due to loss of external power source, power was
supplied by emergency diesel generators. |
|
|
March
31 |
Hamaoka
4 |
Defect
in one reactor pressure signal used to calculate reactor heat output. A
declaration of departure from operational limits according to the Nuclear
Facility Safety Regulations was declared as it was judged that there was a
possibility of an error occurring in the reactor heat output. |
|